Physicochemical and Vibration Analysis of Christmas Tree Four-Way Flange Failure under Fracturing Process

When a wellhead gas production tree in a certain oilfield block fracturing completed 12 layers and 22 layers and then the bottom-up discharge operation was performed, the Wellhead four-way suddenly suffered erosion failure. This is the seventh failure of this operation. In order to obtain the cause...

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Main Authors: Zhaoming Zhou, Dawen Gong, Kelong Yang, Zhong Zeng, Zhou Xiao
Format: Article
Language:English
Published: Wiley 2020-01-01
Series:Shock and Vibration
Online Access:http://dx.doi.org/10.1155/2020/5816205
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author Zhaoming Zhou
Dawen Gong
Kelong Yang
Zhong Zeng
Zhou Xiao
author_facet Zhaoming Zhou
Dawen Gong
Kelong Yang
Zhong Zeng
Zhou Xiao
author_sort Zhaoming Zhou
collection DOAJ
description When a wellhead gas production tree in a certain oilfield block fracturing completed 12 layers and 22 layers and then the bottom-up discharge operation was performed, the Wellhead four-way suddenly suffered erosion failure. This is the seventh failure of this operation. In order to obtain the cause of failure, the chemical analysis, hardness testing, tensile property testing, and finite element structural dynamic analysis are used to analyze the failure of the cross connection. The results of physical and chemical analysis show that the chemical composition, hardness, and tensile properties of the failed parts meet the requirements of the standard, not the problem of the material of the work piece. Due to the high-frequency vibration generated by the three-phase fluid in the pipeline during the discharge process, different types of vibration and deformation of the four-way valve and the valve body occur. The dimensions of the on-site structural parts were measured, and the bolt sizes were found to be different. A finite element model was established based on the measured data for dynamic analysis. Through physical and chemical tests and theoretical calculations, it is found that the cause of failure is the unbalanced load and resonance of the bolt, and the nut undercuts under high-frequency vibration, which causes leakage at the flange connection and eventually causes erosion failure. It is recommended to regularly use an electronic torque wrench to test the pretightening force of each bolt to prevent vibration and failure due to inconsistent pretightening force of the bolts.
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language English
publishDate 2020-01-01
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series Shock and Vibration
spelling doaj-art-ee7517b89a724c1b899aa79cc71e0a942025-02-03T06:43:26ZengWileyShock and Vibration1070-96221875-92032020-01-01202010.1155/2020/58162055816205Physicochemical and Vibration Analysis of Christmas Tree Four-Way Flange Failure under Fracturing ProcessZhaoming Zhou0Dawen Gong1Kelong Yang2Zhong Zeng3Zhou Xiao4School of Mechatronic Engineering, Southwest Petroleum University, Chengdu 610500, ChinaSchool of Mechatronic Engineering, Southwest Petroleum University, Chengdu 610500, ChinaPetroChina Southwest Oil and Gasfield Company, Chengdu 610500, ChinaHSE Quality Surveillance & Inspection Research Institute, CNPC Chuanqing Drilling Engineering Company Limited, Guanghan 613800, ChinaDrilling and Production Engineering Technology Institute of CNPC Chuanqing Drilling Engineering Co. Ltd., Guanghan 613800, ChinaWhen a wellhead gas production tree in a certain oilfield block fracturing completed 12 layers and 22 layers and then the bottom-up discharge operation was performed, the Wellhead four-way suddenly suffered erosion failure. This is the seventh failure of this operation. In order to obtain the cause of failure, the chemical analysis, hardness testing, tensile property testing, and finite element structural dynamic analysis are used to analyze the failure of the cross connection. The results of physical and chemical analysis show that the chemical composition, hardness, and tensile properties of the failed parts meet the requirements of the standard, not the problem of the material of the work piece. Due to the high-frequency vibration generated by the three-phase fluid in the pipeline during the discharge process, different types of vibration and deformation of the four-way valve and the valve body occur. The dimensions of the on-site structural parts were measured, and the bolt sizes were found to be different. A finite element model was established based on the measured data for dynamic analysis. Through physical and chemical tests and theoretical calculations, it is found that the cause of failure is the unbalanced load and resonance of the bolt, and the nut undercuts under high-frequency vibration, which causes leakage at the flange connection and eventually causes erosion failure. It is recommended to regularly use an electronic torque wrench to test the pretightening force of each bolt to prevent vibration and failure due to inconsistent pretightening force of the bolts.http://dx.doi.org/10.1155/2020/5816205
spellingShingle Zhaoming Zhou
Dawen Gong
Kelong Yang
Zhong Zeng
Zhou Xiao
Physicochemical and Vibration Analysis of Christmas Tree Four-Way Flange Failure under Fracturing Process
Shock and Vibration
title Physicochemical and Vibration Analysis of Christmas Tree Four-Way Flange Failure under Fracturing Process
title_full Physicochemical and Vibration Analysis of Christmas Tree Four-Way Flange Failure under Fracturing Process
title_fullStr Physicochemical and Vibration Analysis of Christmas Tree Four-Way Flange Failure under Fracturing Process
title_full_unstemmed Physicochemical and Vibration Analysis of Christmas Tree Four-Way Flange Failure under Fracturing Process
title_short Physicochemical and Vibration Analysis of Christmas Tree Four-Way Flange Failure under Fracturing Process
title_sort physicochemical and vibration analysis of christmas tree four way flange failure under fracturing process
url http://dx.doi.org/10.1155/2020/5816205
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AT kelongyang physicochemicalandvibrationanalysisofchristmastreefourwayflangefailureunderfracturingprocess
AT zhongzeng physicochemicalandvibrationanalysisofchristmastreefourwayflangefailureunderfracturingprocess
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